Flywheel was ready this weekend, so I got a BUNCH of test fitting done.
Stock forged crank flexplate for use with PTT flywheel
I told the machinist to leave a sharp corner on the back side of the crank pilot bore, since the Northstar crank pilot is very short. He did that and stoned the back surface to deburr... Also leaving sharp corners on the bolt holes. I hit those with a countersink, while keeping the sharp corner on the pilot bore.
Lol... I made spacers and snagged longer bolts for the engine stand. While I may be able to install the engine to the stand with clutch, it turns out I still need to remove the engine from the stand in order to install the clutch.
ACT ATGM14 clutch alignment tool worked like a charm, although it's a tight fit into the Northstar crank and difficult to install.
On Summit:
https://www.summitracing.com/parts/acl-atgm14
A key problem I noticed early is that some of the bolt heads hit the flexplate. More on that in a minute.
Here's the transmission fitted:
This is with the stock TOB holder installed inside the bellhousing. This dimension should come down about 0.350" once I get my new TOB holder finished.
Took all the bolts out and it didn't pop off on its own, so nothing is binding.
I've been forgetting to do the one slight block mod required to bolt a Northstar up to a conventional Metric Bellhousing transmission... so here it is graphically:
Here's how flat the diaphragm spring fingers are when the unit is bolted all the way down. This is why I need a taller than stock TOB holder.
The throw out travel is 0.300", and all the manufacturers caution strongly against overtraveling throw out, as that can damage the clutch. I guess the damage is not from the diaphragm spring fingers contacting the disks (possibly from stretching the spring too far?)
I applied strip caulk to the transmission bellhousing. After one failed attempt, I got a measurement by applying the wax paper packing on top of the caulk so it wouldn't stick to the pressure plate cover. You can see the speed holes in the cover in relief in the caulk. This sample calipered at 0.080, so I have even a bit more clearance than estimated. Yay for conservative design and measurements.
Above I mentioned that the bolt heads hit the flexplate. Once I completed the clutch test fit, I looked into that. The anti-rotation features on the bolt flanges all cleared the flexplate. However, this one was REALLY close. That's a 0.005 feeler gauge that didn't make it quite all the way through. A 0.004 feeler will go all the way through, but held by friction.
In this shot, I had already skimmed the bolt heads to clear.
Now, check this out:
This is 180 opposite the one above
Gauge pins tell me that gap is between 0.050 and 0.054. That's almost FIFTY thou larger than the gap on the other side. Considering the tolerances of the flywheel, I think the difference is ENTIRELY in the flexplate. That's 0.050 of axial TIR across the stamped metal part. Keep in mind that GM bolted a 4 lug torque converter that was considerably flatter than that up to this flexplate and... sent it. Enjoy your Cadillac, Sir.
I'm not saying GM's tolerances are crap... This part is a potato chip, but it's a FLEXIBLE potato chip compared to a torque converter. Just pull it flat with the bolts and apparently it lasts well enough that the 4L80E transmissions acquired a reputation for being consummate anvils. Absolute units. Bulletproof. Better is the enemy of good enough, and GM knows EXACTLY where good enough is for this critical interface. Another aspect of this is that the ring gear was probably flat when it had a potato chipped stamping welded to it. That means when the potato chipped flexplate is pulled flat on the converter, the ring gear now has axial runout... and apparently that does not matter either.
Here's fit checking the first article TOB holder on my actual transmission
Here's a video of cycling the same. I didn't realize it until after I sat down to write this post, but it reminds me of something. I'm trying to remember what.
https://i.imgur.com/oFZpDHd.mp4
Bonus shot of the flywheel. Yeah, I was just using 4 bolts for the fit checks. I'll use 8 for the flight assembly. Those are the 0.880 long LS flexplate bolts. Those bolts are the PERFECT length when using only the flywheel. When stacking the flywheel on top of the flexplate, now they have 0.500 thread engagement in a crank flange that's 0.570 thick. I need to call ARP to determine if that's ok or if I have to buy the 1.075 long bolts and trim them down to 0.980 or so. A 25mm bolt would be the PERFECT length for this configuration, but ARP doesn't make any 25mm 11x1.5 flywheel bolts.
BONUS ROUND:
Fucking Green Bitches! hoses finally hit my doorstep over the weekend... 3 months after placing the order
